It's been a while since I updated this and we have some good news and bad news. Fortunately, it's mostly good before anyone has any horrible thoughts!
I managed to get her ship shape ready for a ride on Bank Holiday Monday and it was great to get a few miles in. First stop was at the Super Sausage Cafe:
20180507_095659 by
Matt Bly, on Flickr
Then on to the H Cafe:
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Matt Bly, on Flickr
Total for the day was a reasonable 125 miles, albeit solo (aka billy no mates). It was going well until I got home and was greeted by a rather sorry looking tail tidy:
20180507_131205 by
Matt Bly, on Flickr
I had noticed it drooping after my last ride and hoped it was just my imagination - it wasn't! It was bending exactly where it was identified earlier in another forum and I had hoped that it wouldn't be the case. Unfortunately, it clearly wasn't up to the job so a rethink is required.
Anyway, on to better things and yesterday saw me take a trip to TTS Performance in Silverstone to get a baseline dyno run in before the full system was fitted. It was then on to Baines Racing a mile down the road to get the work done. I was allowed to hang around and film the job. I also picked up a spanned and got involved where I could.
First time with the new Motolug (collapsible) trailer:
20180509_084434 by
Matt Bly, on Flickr
All strapped down
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Matt Bly, on Flickr
Time to start work:
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Matt Bly, on Flickr
Stripped down:
IMG_4644 by
Matt Bly, on Flickr
An assortment of bikes in the workshop:
IMG_4648 by
Matt Bly, on Flickr
You wouldn't believe how much these go for nowadays!:
IMG_4647 by
Matt Bly, on Flickr
Now the plan was to go back to TTS the same day for an 'after' run but we ran out of time and I took the bike home. I was also in a rush to get back out on it and go to the local DOCGB local branch meeting. I was also looking forward to getting a ride in to see how the exhaust had changed things.
As well as the exhaust, I had a Sprint air filter fitted and uploaded the upmap which is essentially a remap suited to the full system. I managed to get out the door at about 1930hrs and the bike was nothing short of transformed! The stuttering at low speed and the unpredictable throttle were gone and it was smooth all the way. It also felt much more tractable at 'normal' revs which is where you are when riding on the road. Within the first 500m I could tell I had done the right thing!
Couple of shots from the meeting:
20180509_195519 by
Matt Bly, on Flickr
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Matt Bly, on Flickr
I believe this is a round case bevel = eye wateringly exclusive and valuable:
20180509_205308 by
Matt Bly, on Flickr
Anyway, back to business. Today, I went back to TTS for the 'after' run. I'll move on to that later but not before more bad news - the tail tidy is no more! It finally cracked along the weak point and when I got to TTS it was in a sorry state. I managed to nurse it to Baines who kindly lent me some tools to remove the whole assembly. I cable tied the number plate to my camera bag on my back and hoped for a lack of rozzers on the way home! Here's the state of it now:
20180510_185600 by
Matt Bly, on Flickr
20180510_185608 by
Matt Bly, on Flickr
After sorting that, I nipped round the corner to Ducati UK for a couple of snaps:
IMG_4671 by
Matt Bly, on Flickr
IMG_4672 by
Matt Bly, on Flickr
IMG_4665 by
Matt Bly, on Flickr