- Joined
- Oct 16, 2023
- Messages
- 76
- Location
- Germany
Hey everyone,
I just did an oil change on my 899 Panigale, and when tightening the M6 bolt on the oil filter housing, I noticed that I couldn’t torque it properly to 13 Nm. At some point, it just kept spinning freely.
I carefully removed the bolt, and a part of the thread came out with it, as you can see in the attached picture.
Now, I need specific solutions to fix this issue and restore the original M6 thread size. What’s the best approach?
Thanks in advance!